GT240 REBUILD

So I blew my GT240 up in the summer. I was pushing along nicely at 70mph ( much faster than I normally go - just ask my riding companions!)…. Then silence …. Seemed to just cut out , no bang or nasty sounds… clutch in , coasted to the hard shoulder to find it seized…




I’ve had it rebored and gone up to the first oversize piston.
Whilst it’s apart I’ve decided to renew main bearing and flywheel side seals and gaskets, and fit a sluk head cowling and vortex fan for supposedly better cooling ( I’m a sucker for new bling )
So what caused the seize? The plug and piston crown do not indicate a lean issue or air leak judging by the colour. I pressure tested it prior to strip down and it holds pressure with no leaks.
There was a dark black oil stain on the main bearing retention plate. (Sucking air and oil in from crankcase?)
The carb was jetted professionally on a dyno.
Fuel tap is fast flow and measured rate is OK
A club member has suggested looking at the float valve size - I’ve ordered a 3.5mm fast flow valve from MB. Feasibly at that speed the engine may have been using more fuel thank the float bowl could supply and it drained..?
Also I gather that compression ratio will increase too with the rebore - should I add a headgasket to compensate for this - the gt240 kit doesn’t usually need one …
Once rebuilt I’ll get it redyno'd and dialed in
Any thoughts on the cause, or rebuild hints and tips appreciated




I’ve had it rebored and gone up to the first oversize piston.
Whilst it’s apart I’ve decided to renew main bearing and flywheel side seals and gaskets, and fit a sluk head cowling and vortex fan for supposedly better cooling ( I’m a sucker for new bling )
So what caused the seize? The plug and piston crown do not indicate a lean issue or air leak judging by the colour. I pressure tested it prior to strip down and it holds pressure with no leaks.
There was a dark black oil stain on the main bearing retention plate. (Sucking air and oil in from crankcase?)
The carb was jetted professionally on a dyno.
Fuel tap is fast flow and measured rate is OK
A club member has suggested looking at the float valve size - I’ve ordered a 3.5mm fast flow valve from MB. Feasibly at that speed the engine may have been using more fuel thank the float bowl could supply and it drained..?
Also I gather that compression ratio will increase too with the rebore - should I add a headgasket to compensate for this - the gt240 kit doesn’t usually need one …
Once rebuilt I’ll get it redyno'd and dialed in
Any thoughts on the cause, or rebuild hints and tips appreciated