by Andie » Sat Mar 26, 2016 6:48 pm
Hello
I've spent the best part of the last two days working on my build.
EDIT I'm not doing very well. can't get it to run for more than 20 seconds.... /EDIT
I've fuelled with BP 97 and 4 p/c semi-synthetic Rock oil. I was advised 4 p/c by the mechanic who built it, who knows his stuff.
Crank case oil checked with scoot level, off stand, and all good. petrol mix getting through to carb fine.
No ignition, just a kill switch that is working fine according to my meter.
1) spark
Its a casatrionic kit fitted to 19 degrees. B7ES Plug gapped at .5
Its not amazingly bright blue but its quite sunny outside.
The kit earths direct to the stator - I could fit a secondary earth from the regulator but it's CDI is earthing fine (black wire to frame).
The plug is wet and has a slight black oily sheen to it ( too rich a mixture?)
I have changed plug and plug cap (all brand new)
2) Petrol/Carb
Carb is a jetex 22 (200cc model) Jets are replacements - 5899-2 atomiser - 45 pilot, 118 main
I've started with the mix screw at 3/4 as recommended by my mechanic.
It won't start from kick over. - I managed to bump start a few times yesterday (i live on a big hill, hard up, easy down...)
It will fire with some throttle to get it to pick up (possible 1/8th + ) - choke in. Fires regularly and does not stutter
It wont tick over when bumped and clutch in without some throttle I've varied the screw from 1/2 in to 1 1/2 out but not much difference.
Could my pilot be too big?
Its flooding and the standard air hose, is getting a lot of spit back fuel in so today I cleaned the carb, and blew through jets with air-in-a can and carb cleaner. Float works fine - moves freely and blocks intake on up position.
The choke jet falls correctly and then clears the chamber so the choke cable seems fine.
3)Compression
Lots of compression! I also dropped the engine down today and checked the inlet (fine) and exhaust studs as they were leaking some specks of black petrol (same as plug). Torqued as the book although I can't get a socket to the flywheel side (U bend won't allow it). no longer leaking. The u-bend and box weren't the best of mates (AF Clubman) and it was also blowing black petrol/oil from the U-bend/box join but I've played around with the clamp and seem to have fixed that.
It bumped again a few times today but not much better. Plug still fouling. Smoke is fairly white but it has been flooding.
It sounds good - like a non too noisy clubman should.
My initial though is that I'm maybe over-jetted (its a 175, with stomach removed from airbox. standard seat, air intake has been cut away) and the mixture is too rich.
I could drill some holes in the airbox if neccesary.
Any advice kindly appreciated!