Since rebuilding my standard li150 it has served me well, reliable starter, good runner. It was a complete engine strip and rebuild, new seals, bearings etc.
Standard li crank, points ignition, li top end oversized at 57.4. 18mm carb airbox etc.
On the way back from Awfully Pleasant last weekend I had problems. Stopped to fill up then took ages to start it, and when it did start I noticed it had a different tone to the engine, all I can describe it as is a bit blowy, deeper sound, almost a bit like running with an open carb. I took it gently from there and after stopping for a coffee a while later couldn't start it again, faffed about and eventually started. Carried on and a while later just going up a slight incline heard a brief squeal/screech and engine cut out. Not really knowing what to do I left it a few minutes then gave it a prod and it started, so carried on. A bit later I stalled at some lights

Took it out an a short local ride out the other night to see how it was, still the different noise and I could swear it's vibrating more than usual through the seat. On way home I gave it a blap, usually I can get the speedo needle tickling 50 if I'm feeling adventurous, but now 45 is tops.
So, I have taken the top end off to have a look.... and need some opinions. No ring pegs missing and to me it looks ok but would like opinions on build up on piston crown and head. I'm thinking drive side oil seal? It's not noticably more smokey, wondering if the squeal/screech was the retaining plate screws.
Don't know if that, and the pics gives enough detail but what do you think? Now thinking just bite the bullet and get the engine off the scoot and on the workbench. This being my first year taking my scooter out and about on a small number of rallies I am still hoping to make Shipston but I am up against it now. I will be Mr Pissed Off from Piss Street, Pisstown, Pissedoffshire if I miss it!!!
The engine was ticking over for 10 mins or so before I stripped it to get some heat in the exhaust to make it easier to get off.
Thanks for looking.



Top plug is the one I took out on way home, bottom is new one but as I mentioned engine was ticking over for a bit before I took it to bits.

