Well had a quick run on the x2 / as266 and actually still too rich

As it was starting to rain decided id get it on the bench with a view to looking over everything, soon as i got the stator side panel off to check with multimeter I notice that the white from the stator to cdi was not connected as it's come loose!
Put that back on after testing the ohms and numbers are within normal, decided to check the timing with the strobe, yep, thats fine too!
So, have popped off the exhaust, ensured that the base, head and exhaust gasket are all ok, no evidence of blow on any and have retorqued the head which was fine. I moved onto the inlet and 2 of the 4 allen head bolts could be tightened up a bit more so could have been some air sucking in there round the gasket instead of just through the carb?
So, now, im going to put it back together and put the jetting back to original and start again once it stops piddling down, so likely to be tomorrow by the look of things :-/